2021-01-02, 07:47 AM
(2021-01-02, 05:27 AM)rastam4n Wrote: Has it been calibrated?
I've done this calibration:
Is this the one you mean? Or maybe there is a different calibration I can do?
Among other things, I deleted my pypilot.conf file, in case there were dodgy calibration transform values. The problem also happens on my boat, and in the shed at home.
I'm wondering if I can hook my MPU9255s to an Arduino and try to read the raw values, see if the heading changes there. Suggestions?