Latest tests :
22-APR-2020 moto.ino version
The actuator is working, but it is very slow.
PMW is 2.29 V
the OUT A / OUT B is 5.39
Then i have changed the servo.speed.max to 100% in the configuration menu, then it's working properly.
PMW is 4.6 V
the OUT A / OUT B is 11.27 V
30-DEC-2020 moto.ino version
Even if i set servo.speed.max to 100% i have low voltages, so the actuator is not working.
In this case my option is to connect the PMW pin of the vnh5019 directly to the 5V pin. I don't know if it's a clean option ? but it's working on my desk
So, now i think it's clear that it's not comming from the vnh5019, but from motor.ino code.
@ CapnKernel : wichh code version are you using ?
@ ironman : Tks for the idea, the issue it's clerarer now. But i am not able to undestant the code differences.
@ Sean : i agrre with CapnKernel, an update with replacement of VNH2SP30 in the code with VNH5019. But maybe it's not relevant if the code is not compatible anymore or have to be updated.
22-APR-2020 moto.ino version
The actuator is working, but it is very slow.
PMW is 2.29 V
the OUT A / OUT B is 5.39
Then i have changed the servo.speed.max to 100% in the configuration menu, then it's working properly.
PMW is 4.6 V
the OUT A / OUT B is 11.27 V
30-DEC-2020 moto.ino version
Even if i set servo.speed.max to 100% i have low voltages, so the actuator is not working.
In this case my option is to connect the PMW pin of the vnh5019 directly to the 5V pin. I don't know if it's a clean option ? but it's working on my desk
So, now i think it's clear that it's not comming from the vnh5019, but from motor.ino code.
@ CapnKernel : wichh code version are you using ?
@ ironman : Tks for the idea, the issue it's clerarer now. But i am not able to undestant the code differences.
@ Sean : i agrre with CapnKernel, an update with replacement of VNH2SP30 in the code with VNH5019. But maybe it's not relevant if the code is not compatible anymore or have to be updated.