I am at wits end now... I rechecked the values between a4 and grd your right i get 0 to 1.1. The resistance between grd and the swipe is about 127k about right. I noticed in pypilot calibration I don't get current / voltage or rudder sense. The actuator works when I use app and responds properly.. I find it odd that the nano is not getting any analogue readings. I might have to just replace the whole controller....... 2hrs later....... I checked the data lines the rpi receive line was broken. once i fix this it worked.. What a jeinous started at the end before i checked the obvious.... now i can test it on op2....
Thanks Sean ...
I plan to mount the pot into the top end of my Pintle with a small shaft. The body of the pot will mounted to the transom. Small out of the way and cheap.
Thanks Sean ...
I plan to mount the pot into the top end of my Pintle with a small shaft. The body of the pot will mounted to the transom. Small out of the way and cheap.